In recent years, the Budryk Coal Mine (KWK Budryk) reached the mining depth of 1300 m, where there is about 160 million tons of coal, including 120 million tons of coking coal (type 35). The task of the Coal Processing Plant complex modernization was undertaken. The article presents the modernization of coal screening, classification and dewatering systems at the KWK Budryk Processing Plant and the implementation of screening of PROGRESS ECO sp. z o.o. SK. The modernization project defined the following technical requirements for all screens in the KWK Budryk Coal Processing Plant extension project: - Vibrating screens with a linear type drive with a drive unit placed on the drive beam of the trommel screen in the form of vibration generators; - Screen drives equipped with a starting-braking device; - The use of main screen drive bearings with a nominal service life of at least 40,000 man-hours; - All work surfaces made of materials with a strength of up to 80 mm grain and abrasion resistance; side strips and sieves fixed in a way ensuring trouble-free operation, and at the same time quick and easy replacement; - Sheets made of stainless steel; - Side walls, beams and other elements attached to them connected with screws using a system protecting against corrosion and elements separation; - The use of a work parameters monitoring and visualization system, i.e. - pitch of the riddle, - bearing operating temperatures and the condition of their wear. Three types of screens were provided: - PWP1-1Z-2,8x6,0 screeners that alternatively perform sieving or desliming processes, - PWP1-2.4x6.0 screening machines performing desliming processes, - PWP1-2.0x6.0 screens performing the classification process.
Control of the technological processes of coal enrichment takes place in the presence of wide disturbances. Thus, one of the basic tasks of the coal enrichment process control systems is the stabilization of coal quality parameters at a preset level. An important problem is the choice of the controller which is robust for a variety of disturbances. The tuning of the controller parameters is no less important in the control process . Many methods of tuning the controller use the dynamic characteristics of the controlled process (dynamic model of the controlled object). Based on many studies it was found that the dynamics of many processes of coal enrichment can be represented by a dynamic model with properties of the inertial element with a time delay. The identification of object parameters (including the time constant) in industrial conditions is usually performed during normal operation (with the influence of disturbances) from this reason, determined parameters of the dynamic model may differ from the parameters of the actual process. The control system with controller parameters tuned on the basis of such a model may not satisfy the assumed control quality requirements. In the paper, the analysis of the influence of changes in object model parameters in the course of the controlled value has been carried out. Research on the controller settings calculated according to parameters T and τ were carried out on objects with other parameter values. In the studies, a sensitivity analysis method was used. The sensitivity analysis for the three methods of tuning the PI controller for the coal enrichment processes control systems characterized by dynamic properties of the inertial element with time delay has been presented. Considerations are performed at various parameters of the object on the basis of the response of the control system for a constant value of set point. The assessment of considered tuning methods based on selected indices of control quality have been implemented.
The environment is the greatest good for the people. Everyone wants to breath air of the best possible quality, whether living in the city center of a metropolis or in a rural area. Air polluted with very fine particles contribute to the negative effect on people’s health and the whole environment. A significant part of air dust pollution comes from the so-called low emissions sources which include: non-standard furnaces, fireplaces, low-efficiency outdated boilers and local heat sources. Since the beginning of Polish Mining Group’s existence, the company actively participates and supports many activities, the aim of which is to improve the air quality by producing and supplying high quality coal for the residential sector. The company has undertaken pro-ecological activities towards creating a new, pro-ecological strategy as well as product offer. The production of an ecological coal assortment is systematically developing but new coal products are also being launched on the market. One of the company’s priorities is the production of thermal coal for the residential sector. Many organizational and technological changes have been made In that area (e.g. the establishmsnt of the Eco-Fuels Production Plant) to ensure a suitable level of production of the highest quality thermal coal.
In this work problems associated with requirements related to pollution emissions in compliance with more restrictive standards, low-emission combustion technology, technical realization of the monitoring system as well as algorithms allowing combustion process diagnostics are discussed. Results of semi-industrial laboratory facility and industrial (power station) research are presented as well as the possibility of application of information obtained from the optical fibre monitoring system for combustion process control. Moreover, directions of further research aimed to limit combustion process environmental negative effects are presented.